Engine Problem on the 2007 MERCURY MILAN
Car problem(s) with the 2007 MERCURY MILAN.
This database includes information received by NHTSA from consumers either directly or as recorded by the Vehicle Safety Hotline. This information may be used by NHTSA during the investigation process.
You may file your own complaint by calling the NHTSA Monday-Friday 8am to 8pm at (888) 327-4236, TTY: (800) 424-9153. You can also file your complaint online.
Problem with Engine
-
Jul 15, 2018 - Brewster, NY - Engine
I WAS DRIVING DOWN A MAIN ROAD WHEN THE CAR JUST LOST POWER COULD NOT ACCELERATE. PULLED OVER TO THE SIDE HAD TO USE E BRAKE TO STOP. TURN OFF CAR TRY TO TURN IT BACK ON AND IT WOULD NOT START ONLY DASH LIGHTS CAME ON. CHECK ENGINE. HAD IT TOWED. MECHANIC DIAGNOSIS 1 OF THE BACK COILS WENT BAD ALONG WITH ECM/PCM. FRIED THE COIL ON THE PLUG FUSE AS WELL. VERY DANGEROUS AND SCARY WHEN YOUR DRIVING IN TRAFFIC ABOUT 50 MILES PER HOUR.CAR HAS 74,000. NO WARNING LIGHT CAME ON BEFORE THIS CAR HAS BEEN MAINTAINED BY FORD WITH OIL CHANGES AND MULTI POINT INSPECTS. THIS SEEMS TO BE AN ISSUE WITH MERCURY MILAN BUT NO RECALLS???
View Details
-
Jan 25, 2018 - Belfast, NY - Engine
THE 2006- 2012 MERCURY MILAN AND FORD FUSION ARE VERY LIKELY TO LOOSE POWER STEERING AND BRAKES. DUE TO THE THE WAY THE BELT TENSIONER IS MOUNTED ON THE ENGINE IS IT VERY COMMON THAT THE BOLT HOLDING THE PULLEY IN PLACE WILL SNAP CAUSING ACCESORIES TO SHUT OFF DUE TO THE BELT FALLING OFF, FORD WILL NOT TAKE CARE OF IT, MYSELF AND HUNDRED OF OTHERS ARE HAVING THIS ISSUE AS I WENT TO FORUMS ONLINE AND FOUND ALOT OF PEOPLE HAVE THE SAME ISSUE, THESE ARE VERY SAFE DEPENDABLE CARS UNTIL THIS STARTED HAPPEING TO ALL OF US, IF YOU ARE UNSURE AS TO IF YOU SHOULD BELIEVE, START A POLL WITH THE OWNERS OF VEHICLES MENTIONED AND OTHERS MADE BY FORD MOTORS, ITS FOUND TO BE VERY COMMON.
View Details
-
Sep 01, 2017 - Fresh Meadows, NM - Engine
TL* TAKATA RECALL. THE CONTACT OWNS A 2007 MERCURY MILAN. WHILE DRIVING 40 MPH, THE VEHICLE SHOOK, SPUTTERED, AND LOST ALL POWER. THERE WERE NO WARNING INDICATORS ILLUMINATED. THE VEHICLE WAS ABLE TO RESTART, BUT WAS TOWED TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED WITH A FAULTY COIL PACK THAT NEEDED REPLACEMENT. THE CONTACT STATED THAT THE INDEPENDENT MECHANIC REPLACED THREE COIL PACKS; HOWEVER, WHEN THE MECHANIC ATTEMPTED TO START THE VEHICLE, THE COIL PACKS EXPLODED AND THE VEHICLE SHUT OFF AGAIN. THE INDEPENDENT MECHANIC INFORMED THE CONTACT THAT THE REPAIRS WERE TOO LARGE OF A JOB FOR HIM AND SUGGESTED THE VEHICLE BE TAKEN TO A DEALER. THE VEHICLE WAS NOT TAKEN TO A DEALER FOR DIAGNOSTIC TESTING OR REPAIRS. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 16V384000 (AIR BAGS); HOWEVER, THE PARTS TO DO THE REPAIR WERE UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE DEALER AND MANUFACTURER WERE NOT NOTIFIED. THE CONTACT HAD NOT EXPERIENCED AN AIR BAG FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 43,200. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.
View Details
-
Aug 29, 2016 - Eunic, LA - Engine
TL* THE CONTACT OWNS A 2007 MERCURY MILAN. WHILE DRIVING 70 MPH, THE VEHICLE DROPPED OUT OF OVERDRIVE AND JERKED FORCEFULLY. THE CONTACT STATED THAT THE ENGINE REVED AND THE SPEEDOMETER FLUCTUATED UP AND DOWN FROM 0-120 CONSTANTLY. THE VEHICLE JERKED BACK AND FORTH EACH TIME THE ENGINE WAS STARTED AND WHEN SHIFTING INTO DRIVE AND REVERSE. THE CONTACT BELIEVED THE THROTTLE CONTROL CABLES WERE FAILING BECAUSE, WHILE IDLING, THE VEHICLE REVED UP TO 2 RPMS. THE VEHICLE WAS NOT DIAGNOSED NOR REPAIRED. THE FAILURE MILEAGE WAS 111,656.
View Details
-
Dec 23, 2014 - New Lennox, IL - Engine
TL* THE CONTACT OWNS A 2007 MERCURY MILAN. THE CONTACT STATED THAT WHILE DRIVING 45 MPH, THE VEHICLE STARTED TO SHAKE VIOLENTLY AND THE VEHICLE STALLED. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC, WHO DIAGNOSED THAT THE FRONT ENGINE COIL WAS SEVERELY BURNED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE VIN WAS NOT AVAILABLE. THE FAILURE MILEAGE WAS 133,000.
View Details
-
Aug 11, 2014 - Pheonixville, PA - Engine
TL* THE CONTACT OWNS A 2007 MERCURY MILAN. THE CONTACT STATED THAT THE WIRES CONNECTED TO THE SPARK PLUGS OVERHEATED AND TRANSMITTED AN INCORRECT CODE TO THE VEHICLE PROCESSOR. THE DEALER REPAIRED THE VEHICLE AND THE MANUFACTURER WAS NOTIFIED. THE FAILURE MILEAGE WAS 82,344. UPDATED 09/15/14 THE CONSUMER STATED THE PROCESSOR FAILED AND SENT AN INCORRECT CODE TO THE COILS, WHICH FRIED THE COILS AND SPARK PLUGS. UPDATED 1/7/2014
View Details
-
Jul 07, 2014 - Lithonia, GA - Engine
BATTERY DIED IN MY 2007 MERCURY MILAN. AFTER REPLACING THE BATTERY THE THROTTLE BODY MALFUNCTIONED. CAR WOULD NOT ACCELERATE AND CHECK ENGINE LIGHT IS ON.
View Details
-
May 29, 2014 - Arlington, TX - Engine
TL* THE CONTACT OWNS A 2007 MERCURY MILAN. THE CONTACT STATED THAT WHILE DRIVING 50 MPH, THE VEHICLE STALLED AS THE CHECK ENGINE WARNING LIGHT ILLUMINATED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC. THE TECHNICIAN DIAGNOSED THAT THE CATALYTIC CONVERTER SENSOR NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 32,000 AND THE CURRENT MILEAGE WAS 97,000.
View Details
-
Mar 28, 2014 - South Pasedena , FL - Engine
TL* THE CONTACT OWNS A 2007 MERCURY MILAN. THE CONTACT STATED WHILE TRAVELING APPROXIMATELY 35 MPH, THE VEHICLE BEGAN TO LUNGE FORWARD WITHOUT WARNING. THE VEHICLE WAS TAKEN TO A PRIVATE MECHANIC WHO DIAGNOSED THAT SIX IGNITION COILS, SIX SPARK PLUGS, AND THE DC COMPUTER NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE VEHICLE WAS REPAIRED BUT DID NOT RECTIFY THE FAILURE. THE APPROXIMATE FAILURE AND CURRENT MILEAGE WAS 33,000. UPDATED 6/10/14 MA UPDATED 08/20/14
View Details
-
Dec 27, 2013 - Fords, NJ - Engine
WHILE FIRST DRIVING MY CAR FROM A STANDSTILL, I NOTICED THE "WRENCH IDIOT LIGHT" ON. THE CAR SEEMED TO BUCK AS IT WENT THROUGH IT'S GEARS. ALSO, THE SPEEDOMETER REGISTERED "0" AT THIS TIME. UPON ENTERING THE HIGHWAY, THE CAR WOULD NOT GO INTO WHAT I THINK IS 4TH GEAR. SEVERAL TIMES, THE CAR LURCHED FORWARD AND THEN THROTTLED BACK TO A LOW RPM, BEFORE RESPONDING TO THE GAS PEDAL. EVENTUALLY, I COULD RUN AT 55 MPH @ 3000 RPM'S, BUT IT WOULDN'T SHIFT ANY FURTHER, EVEN WHEN I WENT FASTER. AT THIS TIME, THE SPEEDOMETER NEEDLE FINALLY REGISTERED MY TRUE SPEED. A COUPLE OF TIMES, THE RPM'S SUDDENLY SHOT-UP AND THEN THE ENGINE THROTTLED BACK. HOWEVER, THE CAR FELT LIKE IT SHOULD HAVE GONE INTO IT'S FINAL FORWARD GEAR BUT COULDN'T. ON LOCAL ROADS. IT SHIFTS EXTREMELY HARD INTO IT'S GEARS. THE WHOLE TIME, THE CAR'S "WRENCH" LIGHT WAS ON.
View Details
-
Oct 04, 2013 - Knob Noster, MO - Engine
PRIOR TO THE INCIDENT DESCRIBED THE CAR WAS ACTING PERFECTLY FINE AND HAD NEVER DIED OR BEEN DIFFICULT TO START. ON THE MORNING OF SEPT 23RD I GOT IN THE CAR I STARTED IT AND IT DIED IMMEDIATELY. I STARTED THE CAR AGAIN AND DROVE FOR APPROXIMATELY 1 BLOCK AND IT DIED AGAIN. I RESTARTED IT AND IT DROVE A COUPLE MORE BLOCKS AND WHEN I STOPPED AT A STOP SIGN IT DIED AGAIN. AFTER THIS THE CAR WOULD START BUT WOULD SHUT OFF AS SOON AS I PUT THE CAR IN GEAR. EVERY TIME THE CAR DIED THE CHECK CHARGING SYSTEM LIGHT WOULD COME ON. THE CAR WAS TOWED TO THE LOCAL FORD DEALER. THE DEALERSHIP RAN THE COMPUTER WHICH INDICATED THE ELECTRICAL THROTTLE BODY WAS BAD. WHEN THE DEALERSHIP REMOVED THE FAULTY THROTTLE BODY THEY COULD NOT FIND ANY DAMAGE THAT WOULD CAUSE IT TO GO BAD. THEY EXPLAINED THAT IT MUST BE A FAULTY PART. WHEN THE THROTTLE BODY WAS REPLACED A CODE INDICATED THAT THE MASS AIR FLOW SENSOR WAS ALSO BAD. THE DEALERSHIP COULD NOT FIND DAMAGE ON THE SENSOR EITHER AND EXPLAINED THAT THE THROTTLE BODY GOING OUT BLEW THE SENSOR.
View Details
-
Jul 02, 2013 - Reston, VA - Engine
INCIDENT OCCURRED AS DRIVER OF MERCURY MILAN 2007 AWD PREMIER VEHICLE WAS DRIVING ON THE HIGHWAY AT A SPEED OF AROUND 50-45MPH. THE CAR BEGAN TO SHUDDER AND VIBRATE. VEHICLE DASH LIGHTS AND ENGINE CUT OUT COMPLETELY IN THE MIDDLE OF DRIVING, DRIVER MANAGED TO MAKE IT SAFELY TO THE SIDE OF THE ROAD. CAR WAS TOWED TO NEARBY AUTO SERVICE FACILITY. UPON INSPECTION THE PCM MODULE WAS FOUND TO BE DEFECTIVE. THE PCM MODULE SHORTED OUT ALL 6 IGNITION COILS AND DUMPED FUEL INTO THE CONE OF ONE CATALYTIC CONVERTER STOPPING IT FROM WORKING. FURTHER INVESTIGATION SHOWED THAT THE PCM MODULE IS A DOCUMENTED PROBLEM FOR A VARIETY OF MAKES AND MODELS OF FORD/MERCURY CARS. THE PCM MODULE WAS ALSO ON BACKORDER FROM MULTIPLE LOCATIONS. THE MECHANIC ALSO MADE EXTENSIVE INQUIRIES ABOUT THE CURRENT PCM MODULE AND THE BACKORDERED PCM (WITH NEW DRIVERS AND PROGRAMMING). THE MECHANIC WAS INFORMED THAT PLACING THE OLD PCM IN THE CAR WOULD RESULT IN SIMILAR ELECTRICAL COMPONENTS BEING COMPROMISED BECAUSE OF THE FAULTY VERSION OF THE PCM. TOTAL BILL RESULTED IN $3600, GROSS SAFETY HAZARD FOR THE CAR SHUTTING DOWN ON A BUSY HIGHWAY. IT IS MY HOPE THAT FORD BEGINS TO EVALUATE THIS AS AN ISSUE AND PUSH IT TO THE RECALL LIST BEFORE SOMEONE GETS SERIOUSLY HURT. LASTLY, THE BACK ORDERED PART MEANT THE CAR WAS NOT AVAILABLE TO DRIVE FOR OVER A MONTH.
View Details
See similar problems for the following vehicle(s)